Displaying 176 - 199 of 199

Report TitleIncident TypeYearWeather ConditionsEnvironmentLocation of incident/near miss
Incident Report 05/20/2017IncidentClearI just had the guide plate come off from the bottom of the B.O.P'S while using rig lock and land directly onto a guys head,shoulders,and then his arm. Please make this correction to the guide plate so it doesn't happen to you or your guys. It happened because the hydraulic hose got tangled behind the latch and unlatched it.Loving, New MexicoNone
Incident Report 10/20/2016Near MissUnknownWhile perforating a well for Plug & Abandonment, high levels of Carbon Monoxide (CO) were detected on the platform.UK Sector N. SeaChoose not to answer
Incident Report 10/20/2016Near MissNot significantFollowing a TCP job, the down-hole retrievable packer was unseated, and any produced gases were circulated out. During circulation the Carbon Monoxide (CO) and H2S alarms activated in the areas of the gas buster and mud lines. The rig crew was mustered twice in case an abandonment was necessary.Offshore Trinidad & TobagoPercussion activated - mechanical
Incident Report 10/20/2016Near MissCalm no windsHigh levels of Carbon Monoxide (CO) were detected during perforating operationsHarvest Platform, Santa Barbara County, California, USAChoose not to answer
Incident Report 10/20/2016Near MissCalm no windsHigh levels of Carbon Monoxide (CO) were detected during perforating operationsHarvest Platform, Santa Barbara County, California, USAChoose not to answer
Incident Report 10/20/2016Near MissUnknownCarbon Monoxide (CO) was detected at surface during wireline perforating operationsCalifornia, USAChoose not to answer
Incident Report 10/20/2016IncidentClear summer dayWhile making several perforating runs to perforate water bearing zones, three members of the rig crew working on and around the wellhead were overcome by Carbon Monoxide (CO) gas produced as a by-product of the perforating process. Water was being flowed from the wellhead at surfaceVintage Petroleum, Ventura County, California, USAChoose not to answer
Incident Report / Experience Transfer Maersk Giant 03:40 11 Aug 2015IncidentUnknownM_rsk Giant 03:40 11 Aug 15 Facts: Pressure increase after setting of perforating guns 2 persons on drill floor to verify guns shoot off. As guns went off, they realized something went wrong and escaped to safe position. Drill string was forced upward, string parted and landed on drillfloor The rest of the string went into hole. Parted drill pipe apx. 1 single joint. Causes: Pressure build up after/during fire perforating guns.UnknownUnknown
Incident Report 07/01/2018Near MissOffshoreFreezingNightHouston
Incident Report 07/06/2018Near MissOffshoreClearNightBUCURESTI SATRAIESTI
Incident Report 07/16/2018IncidentOffshoreSnowNightrig floor
STxNear MissLandClearDaygun loading area
Incident Report 07/27/2018IncidentLandCloudyNightWTx
Incident Report 07/27/2018Near MissLandClearDayGOM
Surface pressure effectsrig floor
Incident Report 07/19/2017West Texas
Incident Report 05/20/2017Loving, New Mexico
Incident Report 10/20/2016UK Sector N. Sea
Incident Report 10/20/2016Offshore Trinidad & Tobago
Incident Report 10/20/2016Harvest Platform, Santa Barbara County, California, USA
Harvest Platform, Santa Barbara County, California, USA
Incident Report 10/20/2016California, USA
Vintage Petroleum, Ventura County, California, USA
Incident Report / Experience Transfer Maersk Giant 03:40 11 Aug 2015Unknown
Report TitleIncident TypeYearWeather ConditionsEnvironmentLocation of incident/near miss